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蜜桃视频中文字幕脫硫係統常見問題及解決方案
一、化學吸收係統故障
1、 Chemical absorption system malfunction
(一)吸收劑失效
(1) Absorbent failure
在蜜桃视频中文字幕脫硫的化學吸收係統中,吸收劑失效是常見問題。判斷吸收劑是否需要再生,有著明確的標準:
In the chemical absorption system of biogas desulfurization, the failure of absorbent is a common problem. There are clear criteria for determining whether the absorbent needs to be regenerated:
氧化鐵作為吸收劑時,當硫容超過 30wt%,可采用曝氣再生的方法,曝氣時長為 4 小時;
When iron oxide is used as an absorbent, when the sulfur content exceeds 30wt%, the method of aeration regeneration can be used, with an aeration duration of 4 hours;
對於 NaOH 溶液,若其 pH 值低於 8.5,就需要補加濃度為 20% 的新液;
For NaOH solution, if its pH value is below 8.5, a new solution with a concentration of 20% needs to be added;
活性炭作為吸收劑,一旦穿透硫量大於 15mg/g,則需要通過 350℃的熱再生方式恢複其活性 。
Activated carbon, as an absorbent, needs to be restored to its activity through thermal regeneration at 350 ℃ once its sulfur penetration exceeds 15mg/g.
(二)設備腐蝕
(2) Equipment corrosion
設備腐蝕同樣影響著化學吸收係統的正常運行。為此,製定了一套全麵的防護方案:
Equipment corrosion also affects the normal operation of chemical absorption systems. For this purpose, a comprehensive protection plan has been developed:
采用厚度不小於 3mm 的玻璃鋼內襯,增強設備的防腐蝕能力;
Adopting fiberglass lining with a thickness of not less than 3mm to enhance the corrosion resistance of the equipment;
對於關鍵部件,選用 316L 不鏽鋼材質,提升其耐腐蝕性;
For key components, 316L stainless steel material is selected to enhance their corrosion resistance;
安裝陰極保護係統,並將電位控製在 - 0.85V,有效降低設備被腐蝕的風險。
Install cathodic protection system and control the potential at -0.85V to effectively reduce the risk of equipment corrosion.
二、工藝控製問題
2、 Process control issues
(一)硫泡沫處理困難
(1) Difficulty in handling sulfur foam
硫泡沫處理困難會阻礙蜜桃视频中文字幕脫硫係統的高效運行。為解決這一問題,可采取以下優化措施:
The difficulty of sulfur foam treatment will hinder the efficient operation of biogas desulfurization system. To solve this problem, the following optimization measures can be taken:
添加 50ppm 的有機矽類消泡劑,減少泡沫產生;
Add 50ppm silicone defoamer to reduce foam generation;
改進浮選裝置,采用溶氣氣浮工藝,提高硫泡沫分離效率;
Improve flotation device and adopt dissolved air flotation process to improve sulfur foam separation efficiency;
安裝自動排硫係統,通過液位聯動實現硫泡沫的自動排出,提升處理自動化程度。
Install an automatic sulfur removal system to realize the automatic discharge of sulfur foam through liquid level linkage and improve the degree of processing automation.
(二)尾氣 H2S 超標
(2) Excessive H2S in exhaust gas
當尾氣中 H2S 出現超標情況時,需及時采取應急處理措施:
When H2S exceeds the standard in the exhaust gas, emergency measures should be taken in a timely manner:
迅速啟動備用吸收塔,增加吸收處理能力;
Quickly activate the backup absorption tower to increase absorption processing capacity;
將循環量加大 30%,增強對 H2S 的吸收效果;
Increase the circulation by 30% to enhance the absorption effect of H2S;
對在線分析儀進行檢查,校準零點,確保檢測數據的準確性,以便更好地控製脫硫過程。
Inspect the online analyzer, calibrate the zero point, and ensure the accuracy of the detection data to better control the desulfurization process.
三、運行維護要點
3、 Key points of operation and maintenance
(一)日常監測項目
(1) Daily monitoring items
日常監測是保障蜜桃视频中文字幕脫硫係統穩定運行的重要環節,各參數有著嚴格的控製範圍與檢測頻率:
Daily monitoring is an important part of ensuring the stable operation of the biogas desulfurization system, and each parameter has strict control range and detection frequency:
入口 H2S 濃度需實時監測,控製在小於 5000ppm;
The concentration of H2S at the inlet needs to be monitored in real-time and controlled below 5000ppm;
出口 H2S 濃度每小時檢測一次,確保其低於 20ppm;
The H2S concentration at the outlet should be detected once every hour to ensure that it is below 20ppm;
係統壓差每班檢測一次,要求小於 15kPa。
The system pressure difference should be checked once per shift, with a requirement of less than 15kPa.
(二)關鍵設備維護
(2) Key equipment maintenance
關鍵設備的維護關乎係統的長期穩定運行:
The maintenance of critical equipment is crucial for the long-term stable operation of the system
洗滌塔:每月檢查填料,保證破損率低於 5%;每個季度清洗噴頭,確保其流量偏差不超過 3%。
Washing tower: Check the packing every month to ensure that the damage rate is below 5%; Clean the nozzle every quarter to ensure that its flow deviation does not exceed 3%.
再生槽:每周檢測氧化還原電位(ORP),需維持在 + 100mV 以上;每半年更換曝氣管,當曝氣管通量下降超過 15% 時,及時進行更換 。
Regeneration tank: Check the oxidation-reduction potential (ORP) weekly and maintain it above+100mV; Replace the aeration tube every six months, and promptly replace it when the aeration tube flux decreases by more than 15%.
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